MR2 Turbo problem
Uploader Comments (AndrewZorn)
All Comments (67)
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sup broo i just fixed my car!
i think u have the same as me
i had a clogged cat!
the one below the turbo check it man
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HI man! well im having kinda the same problems with my mr2
i acelerate and it gives turbo lag only 10 psi's
and i dont get alot of power
plzz msg me if u fix this
ill msg u if my mechanics find the problems
thanks!
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Hey there Andrew, i'll give you the head's up on Mr2's.... All the answer's given to you are most probably right but all the answer are wrong !!!! The main intake hose from ur Air Flow meter to turbine is most probably britalled it's way off after replacing it with the K&N filter, if that hasn't been damaged in any way it will be your Air Flow meter..... That's why your car is running toooo Rich..... that's why you are also getting rpm surging..... AIR FLOW METER !!!!!
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can i make a suggestion?,replace your turbo with an original TRD one.i had one of those and its cool.now i have a replaced turbo which puts out 200hp or something
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You could have needed a new clutch because if your clutch is worn out or there is basically no clutch plate left that it would cause the clutch to slip so bad you can floor it and it doesn't to much of any thing.
thats why u use stock bypass valve. if BOV, then make sure its a good one. cheap bovs are for 140hp shitboxes :)
briinums 1 year ago
@briinums It is the Synapse BOV, which is generally considered a good one. I just got unlucky, it got gunked up... if it happens again, I know it was something bad actually running through it, if this never happens again, it was just a one-time-thing. So far about 4 months (a full 'season' considering when this happens) of no problems.
AndrewZorn 1 year ago
@AndrewZorn
oh, then it must have been a total brain wash for you when seeking for the problem as you wouldnt expect a synapse failing :D did they give you a free replacement?
briinums 1 year ago
@briinums I didn't expect a new anything to be the problem... and like I said, it got gunked up somehow, it was cleaned and works perfect now.
AndrewZorn 1 year ago
Pretty sure I've FINALLY fixed this...
The blowoff valve, which WAS REPLACED, was getting stuck.
3 months of hot weather since the fix and I have not had even a hint of this issue.
AndrewZorn 1 year ago
The pros are now saying it is timing, but timing that is frequently messed up due to *some* problem with the ECU. Found out an EEPROM wasn't properly seated, that didn't fix it.
AndrewZorn 3 years ago