Uploaded videos
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run3_e.MP4
sharpemt24
21 views
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run2_e.MP4
sharpemt24
15 views
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run1_e.MP4
sharpemt24
13 views
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run_3.AVI
sharpemt24
10 views
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run_2_close.AVI
sharpemt24
14 views
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run_1.AVI
sharpemt24
12 views
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Sharp right turn
sharpemt24
50 views
After adjusting the frequencing and duration of the 'corrective' steering, the car passed my sharp-right test. Also - the car is set to stop within about 10-12 feet of the ...
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Turning Left
sharpemt24
46 views
Successful left-turn test
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Hitting a Tire
sharpemt24
44 views
The car was not set to correct it's path frequently enough to avoid this car.
Basically the angle was too sharp, and correction steering was not occurring frequently enough.
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GPS Arduino Car Testing
sharpemt24
1,693 views
Testing the car indoors, no GPS for the logic.
Just forward for 1 second while turning right, and backward for 1 second turning left.
Confirmed that my h-bridge is workin...
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